I need to get this data log stuff. For one though, I am pretty sure mine is not CTS cause I purchased a brand new one and it did nothing (but I haven't looked at all the wiring to the CTS yet).
Well, looking more at it this weekend, I think that "3rd plug" I talked about isn't really my problem, because the more I looked at it, it really only goes to the ALDL, Check Engine light, VSS, stuff like that. Nothing really dealing with just start up and running/idle. So I think I need to look at our original grafting of my original harness and the TBI harness stuff again and make sure it is all in line.
Would a bad ground cause something like this too? I'm wondering if one of the grounds just sucks so it's causing the computer to freak out a little
Well, looking more at it this weekend, I think that "3rd plug" I talked about isn't really my problem, because the more I looked at it, it really only goes to the ALDL, Check Engine light, VSS, stuff like that. Nothing really dealing with just start up and running/idle. So I think I need to look at our original grafting of my original harness and the TBI harness stuff again and make sure it is all in line.
Would a bad ground cause something like this too? I'm wondering if one of the grounds just sucks so it's causing the computer to freak out a little



. ssyork was kind enough to send me his TBI computer out of his rig (cause he is swapping a 5.3 in currently). He had a custom chip burned for his cause he had a vortec fuel pump and a 454 TBI unit, but I decided to just plug it in and see what happens. I could tell immediatly that it was cranking and trying to start way better, but didn't want to start, so I swapped out the chip's from my stock ECM. It still had a little bit of a hard time starting up and idling right off the bat. We had an old TBI unit sitting around, so we decided to swap the IAC too, and that seemed to help out quite a bit.
It seemed like after a little bit the computer started to learn and it started to run better and better. So I decided to pull it out of the shop and start to drive it around. The thing was smoking out the exhaust like crazy, especially just out of the right bank, to the point we were thinking maybe the valve's weren't seating all the way. But I just decided to take it out and stretch it's legs a little. After getting it up to 50 or 60 mph it stopped smoking!! And seems to be running a lot better. So I am going to just put the dash back together and run it for a while. "