So, update time.
Verified that all the wiring we were worried about is connected correctly, so far it looks like I built the wiring harness correctly.
I moved the injectors around (which involves dismantling the top of the engine) and no change there, but it started running really bad, then wouldn't start at all.
Eventually I decided to try replacing the distributor (again) and it fires right up! However, while setting g the timing I caught one of the plug wires arcing to the head. So I pulled the supercharger (again) so that I could replace the plug wires. Now it runs great again! No more misfire!
I still have the idle issue though, and a scan tool shows it running way lean, even though the exhaust smells rich. I decided to replace the o2 sensors to see if that was the issue and found this:

The v band is obviously leaking. Both sides were the same. You can see the o2 sensor just inside. Now, this is downstream from the sensor, but it's pretty close. Maybe that is the cause of my bad reading?
Gonna put it back together tomorrow with some copper rtv and see if there is any improvement.
Verified that all the wiring we were worried about is connected correctly, so far it looks like I built the wiring harness correctly.
I moved the injectors around (which involves dismantling the top of the engine) and no change there, but it started running really bad, then wouldn't start at all.
Eventually I decided to try replacing the distributor (again) and it fires right up! However, while setting g the timing I caught one of the plug wires arcing to the head. So I pulled the supercharger (again) so that I could replace the plug wires. Now it runs great again! No more misfire!
I still have the idle issue though, and a scan tool shows it running way lean, even though the exhaust smells rich. I decided to replace the o2 sensors to see if that was the issue and found this:
The v band is obviously leaking. Both sides were the same. You can see the o2 sensor just inside. Now, this is downstream from the sensor, but it's pretty close. Maybe that is the cause of my bad reading?
Gonna put it back together tomorrow with some copper rtv and see if there is any improvement.

