My room mate (years ago) made wooden platforms that were the same height as his four corner scales. He would jack his IMCA Modified up, set it on the wood platforms, and then roll it onto the scales.
Martin
Martin
My room mate (years ago) made wooden platforms that were the same height as his four corner scales. He would jack his IMCA Modified up, set it on the wood platforms, and then roll it onto the scales.
Martin

I think with independent suspension that would be more important to roll it around some, because the suspension cycles in a sideways arc as it is compressed, so not being able to slide would impact the settling. With solid axles there should not be any side loading of the scale and if one axle is in "park" and the other free to roll it should be pretty darn close.
Is the nitrogen and tire pressure in your shocks even pressure? Because that should make more of a difference in corner weights than the floor being off 1/4" or something when the 4 corners are sitting on a spring.
If its sitting on the solid stops, then that would make a huge difference just a tiny amount of error, and is totally understandable.
Thank you David.A long overdue thankyou, I have followed along without comment, but your work has inspired me to think through whatever project I am tackling, deepen skills and achieve a better result. Ethically I don't involve myself with facebook, in addition I have always found forums to be superior learning and information tools. Somewhat limited with CK5 recently as I cannot justify the dollars to access pictures. Greg, once gain my thanks for all the years of contribution and my best wishes for the future- Cheers David
The last 12 months have been filled with lots of changes and forward progress on the MightAsWellK5. It's going to take several posts to get through all of this so please be patient as I organize thousands of photos and try to explain everything that has been happening...I've been wanting to buy that same system. It's on my Christmas list hopefully.2023.07.04 - UPDATE! - MULTI-PART UPDATE....
OK, time for the annual July 4th build update.The last 12 months have been filled with lots of changes and forward progress on the MightAsWellK5. It's going to take several posts to get through all of this so please be patient as I organize thousands of photos and try to explain everything that has been happening...
When we last checked-in, the main efforts were around getting space for the hydroboost and framerail headers. The amount of effort and time required to hand-render the parts proved to be the last straw, and a major decision was made to move the capability of the shop forward. There had to be a faster way to revise and test designs and if this truck was EVER going to run under it's own power again, something drastic had to happen.
An order (backorder actually) was placed with Langmuir Systems for a complete 4' x 3' CNC Plasma Table solution... which arrived in early September of last year.
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The kit was very complete, and the support for this product both from the company and the internet enthusiast groups is phenomenal. It's also at a price point that makes it untouchable by any other "hobbyist" machine out there.
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One of the hardest parts of adding this new tool to the workshop was learning all the new software for drawing and CNC cutting. This was my first time creating G-Code so it was a pretty slow process initially. Started off with a very simple goal of cutting out a plate with the layout of the GMT-800 steering box bolts
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And eventually, the machine was working as expected and cutting out parts WAAAY faster than I could have ever hoped to do manually.... with much higher accuracy as well (obviously)
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Having this machine was clearly going to be a game changer.......
STAY TUNED FOR PART 2.....3.....4......5
-G

snip ... broadcasting information out onto the internet and wondering if anyone even notices...
...I've seen what you can do without one, I can't wait to see what you come up with and build WITH one.



This will give all sorts of options later on... and will be fun to play with when this engine finally hits the dyno stand a few weeks from now. 




Is the nitrous in lieu of turbos cause of the engine bay space? Or just that the motor in this kind of vehicle isn’t likely to spin high enough to take advantage of turbos?It happens.
For every story of a build plan... there are always those surprises and drama that force you to make tough decisions and either continue to fight or give up in defeat. Such was the case when the 502BBC arrived in Heath's shop (Volcano Manifolds) in a big 1075Lb wooden crate.
The unboxing and inventory of parts was going great... the theory was that the engine could be stripped-down and inspected and then the new cam, heads and other parts could be fitted to the existing shortblock. Not an effortless amount of work, but a straightforward project that would take a modest number of hours to complete. Everyone was in great spirits as the engine started coming apart and then the phone rang...... "Hey, Greg... uh, I got the heads off your engine and we need to talk.....". That's never a phone call you want to get..... As it turns out, there was some minor water staining in the #3 cylinder.
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You can see the cross-hatching in this picture.... the bore itself is pretty clean and nice, but the stain runs deeper than the hatch pattern and Heath indicated that you can "feel" it with a fingernail. So was not just a cosmetic issue, but could also result in some oil blowby and/or compression loss past the rings. This was a gut punch on a couple of fronts.... obviously, he could address this with new machining of the block but the machine shop was backed-up with work for almost 6 months... so this entire project would basically be dead for most of this year until we got that work completed. Add to that the actual costs of a full block machining, and the cost of new oversized pistons to go with it and it was starting to feel like we needed to consider other options.
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Ultimately, the we decided that we just couldn't afford to wait 6 more months to get this project moving forward and ordered up a brand-new GM factory 502 short block. It was delivered 2 days later to Heath's shop and was used as the basis for the engine build from that point on. When you see that the engine pictures suddenly go from Chevy orange to basic black... this is why.
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With the first bit of drama behind us, Heath started working the other details. The Brodix heads got a mild bowl blend job and all valve seats were checked for proper seal to make sure that there would be no compression loss...
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A new Volcano single-plane high rise manifold was also fitted to the engine with careful port-matching to the heads. A gasket is used to make the impression and then the intake is opened up to create the exact shape of the intake ports on the heads.
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From the inside of the plenum (looking down) you can see the parting line between the intake and the cylinder head, and the nice clean transistion between these parts. Although not visible in this photo.... Heath also added one of his hidden nitrous kits in the base of the manifold.... because "Might As Well"This will give all sorts of options later on... and will be fun to play with when this engine finally hits the dyno stand a few weeks from now.
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Top view shows the heads after the matchporting... all cleaned up and ready for the manifold to be installed for good. If you look closely you can also see the custom timing cover with the crank trigger setup for the Holley DIS. This was a really stealthy way to get full spark control on this engine and since the Dominator EFI setup already supports it.... the only thing we needed to do was buy the parts to attach... and of course, 8 coil packs which now need to be hidden somewhere out of sight (because "stock") LOL
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This is the current state of engine as of today. The EFI is installed and some of the wiring harnesses are now in place... mostly running through the hollow section of the intake manifold to keep the visual look as clean as possible. The Oil Pump drive is installed where the distributor used to live... since there is no longer a need for a conventional distributor.
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Current schedule (according to Heath) is about one additional week to get the nitrous lines fitted and get the rest of the EFI and sensors set up. After that we are both at the mercy of his local dyno shop to schedule us in for the engine break-in.....leak checks.... and finally some power pulls. Both normally aspirated and with a healthy shot of nitrous as well. Need to make sure that we get lots of photos and videos of that process to share..... with any luck this will happen by the end of July.



PART 3: 502 BIG BLOCK BUILD AND HEARTBREAK.....
Is the nitrous in lieu of turbos cause of the engine bay space? Or just that the motor in this kind of vehicle isn’t likely to spin high enough to take advantage of turbos?
Nice to see you getting set up on the drivetrian. However, the one thing I was eager to see is your custom axles shafts for your 9"/MOG axle assemblies.

