2 victories and 1 stalemate today.
Installed new plug wires; MSD Super Conductor 8.5mm wires.
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Spendy, but I wanted to be sure. Victory #1, the feedback in the radio is gone.
I also changed out the gasket under the throttle body with this one. Holley 108-10
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I trimmed about 1/8" off 1 side and the front of the inside opening so none of the gasket was hanging over the edge. Unfortunately it didn't eliminate the whistle noise. So that's a stalemate.
I'm just going to let it go for now. If I'm listening to music at my typical volume, I don't even notice the noise. If it really bothers me, I just have to move the throttle a few percent and it goes away.
Victory #2 came at the gas station. With the carb I was getting 11.25 mpg consistently on my typical daily commute. On a few trips with almost exclusively highway driving, it pushed into the 13's. Today I calculated 14.2mpg after my commute driving. That's solid 3mpg improvement! If that holds, I'll save $600/yr with gas at $2 a gallon.
That's a better payback than I expected. I thought I would see mpg improvement, but not enough to pay for the cost of the EFI in less than 5 years. I'm pretty happy about that.
On the whole, I'm getting to a happy place with the PF4. Unfortunately the whole business with the wire shorting on the exhaust causing it to randomly die, has delayed my satisfaction with the PF4. Almost like a traumatic experience, it's taking me a little while to get to the place where I can drive it and not be holding my breath waiting for it to die. The kicker is, that was all my fault.