Trip report.
Left the house Sunday the 5th. 588 miles with one gas stop and 2 old man stops. The truck ran great. It developed an exhaust tick about 2 hours in. I kept going, because it sucks to work on hot exhaust. Traffic sucked in numerous places. I every Slug Utility Vehicle, with dad, mom and multiple rugrats and 5 bicycles hanging on the back, were on the road. Fall break this week in our area.
Ran the truck at 75 to 80 mph for most of the trip. For the blue state people, speed limits out this way are 70 to 75 mph on the open roads. It did not use any oil. Fuel gauge would not go above 3/4 tank. Has been this way for a while and I can not figure out why. More on this later. The last 150 miles was running in torrential down pours. The wipers need to due better. I think I have a solution.
Monday morning junior and I went to O'Reilly's by his house and bought some Cometic all steel gaskets. The gaskets in it were fiber multi layer. Pulled the dog house out and saw the front 2 bolts were 1/2 out.

Tightened those and the rest of them as they all could use some twisting. Fired it up and the tick was still there, but at the back port.

Those 2 bolts were the tightest. At least it is supper easy to get the the head on that side. Swapped the gasket that was clearly blown out of the top. Torqued the bolts to the click/click of my tongue. Junior was laughing.
We went for a drive down highway 90 to get gas. I should have filled up the night before, because I was low according to the gauge. Put 27 gallons in a 40 gallon tank. I received a text message from a friend in Tennessee. He saw me go by. Small world. Not a lot of cars out mid-morning on Monday. We drove down to where my friend was and hung out there to watch cars go by.
Monday evening I pulled the tank cover. I disconnected the fuel sending unit wire, ran one from there to the gauge wire in the dash and checked the continuity. The factory harness wire showed 27 OHMs. Never going to show full with that. When the temp wire was hooked to the gauge, it showed full. Put it back together with the factory wire and just ran it.
Tuesday morning we went to a senior care facility for a parade lap through for the old folks. I asked if burnouts were allowed. "YES". So I let the others know. Every car there did one in their parking lot. I finally got to use the line lock. The truck pushed through the brakes twice. I did lay down some 20 foot stripes.
The weeks stuff is listed in the Cruising the Coast thread.
Headed north at around 10:30 am Saturday. The plan was to be in Guntersville AL by 5:30 ish. The Slug Utility Vehicles were out again. Maps showed me getting there by 4:30, but I had a stop to make and would need to stop for gas. My nephew in California named his son Henry. They call him hank. So I had to stop at the Hank Williams Sr. child home and museum. I was barely able to get into the parking lot. Gat was 8 feet wide and the trailer hitch drug hard into the pavement. Museum was OK. Picked up some Hank Williams to send to the great nephew. Leaving, I had the hitch hang up in the curb. I had to back up and get a run to get over it. No way to go out at an angle due to the fence.
According this sign, he was not Henry. My nephew did not know this. I told him I was going to call his son Hiram.
With all of the traffic, I did not make it to Guntersville until a little after 6pm. Met
@TuckerK5 and his wife for a very nice meal. He reserved a hotel for me, so I did not have to deal with that when I got there.
Cool city. He said it was the biggest lake in AL. View from the room. This is small section the lake.
He came by Sunday morning because we forgot to take a picture. So he gave me a tour of his Mill. cool operation. A lot of custom automation to make it more efficient. Big operation.
Headed north after another fuel stop. Those $100 bills are going fast. Arrived at Rocket City Dragway for day Zero of Sick Smokies. See the "All things drag racing" thread for the pictures. A lot of really nice builds, and some "what were you thinking?" Test and tune was supposed to start at 1:30pm. Did not start until 2:45. Saw the class A, B and C cars run. Left at 4pm because I was 4 hours from home. As much as I hate driving at night, especially this truck, with all of the tinted flat glass, I kept going. The reflections in the windows suck.
I was cruising at speed limits because of the traffic flow. Stopped once for an old man issue. It was dark out. When I pulled of of the freeway, I thought I did not have headlights. Hit the high beams, the light changed, but was not better. Right headlight looks good for halloween. Dim and orange. Goes out on high beam. Checked the ground and the plug. It seems to be the bulb. So I motored on.
Pulled in at 9:10 pm. I forgot about the time difference.
The repair list.
