Mark and Scott got here at about 10. With some clea re nice issues on the the clutch fork worked out, it went in smoother than I thought it would. Had to slide it back a 1/4 of an inch once to get the ears over the throw out bearing. Then it tightened down and we pulled the jack out.
Was trying to check the bearing movement and adjustment. Something weird was going on. The clutch brake has never worked as long as I have had the truck. This was the time to figure out why. The clutch rod from the pedal link to the fork arm was a cobbled together piece of crap. Now it is a shorter cobbled together piece of crap. But the clutch was still not right. When the needle was pressed, the arm would rotate the clutch shaft some, but then the shaft would stop as soon as the clutch started releasing?????
The clutch arm has and indexing bolt on the shaft. Notice the arm and shaft were not working together. Took the arm off because I remembered the shaft had a key way. Looked at the arm and yep, it has one also. Arm was never removed from the truck.
I cut a new key and realized at that moment that the weird piece of metal I found in the sweepings one day was the old key, that had been sheared length wise at some time. New key fixed everything.
They got one air tank installed and hooked up while I tried to find the second bracket for the other air tank. We looked everywhere. Even went through the reach. No luck. So I made a new one. Should have it all back together Monday. I hope.
Thanks again to Scott and Mark. This would have been a nightmare without them. The brotherhood at work.