The crank is almost ready to go!
Well, I finally got to use the manual lathe at my friend's shop. It has been tied up with paying jobs for the last couple of months, so I haven't been able to machine my crank to fit my block.
For those who haven't read the whole thread, I bought a brand new GM 6.5 crank for my engine project. The problem? 6.5's all have one-piece rear main seals, whereas my 6.2 block uses a 2-piece seal. I bought it hoping I could make it fit, and when I measured it after I got it I confirmed that it would work with the proper modifications. Why not simply buy a new 6.2 s-pice seal crank? Simple - there aren't any to be had. All the NOS GM cranks have dried up, and all current production, whether AMG/GEP or Chinese (
) are one-piece seal types. So, if you want a new crank for your 2-piece seal 6.2, this is the only way to get one.
Here's what a stock 6.5 crank looks like (this is a pic of some Chinese POS on Ebay - I never got a good pic of mine before I machined it ):
You see that the seal surface is slightly larger than the flywheel hub.
Now, let's see what a 6.2 2-pice seal crank looks like:
Here's a closer look at the seal area:
You notice that next to the rear main journal is an oil-slinger flange, and then the seal surface, followed by the flywheel flange. The seal surface has a bit smaller diameter than the main journals. The distance between the counterweight cheek and the seal surface cheek is greater on the 6.5 crank vs the distance from the counterweight cheek to the oil slinger cheek on the 6.2 crank. This means that I could not duplicate the entire oil slinger. Instead, I ended up with a "mini-slinger" that comes very close to the block at it's outer edge. This should make a decent dynamic seal and give good oil control. Here's what it looks like in the block:
Here's a closer look:
You can see where the original radius started on the main journal side. I made the diameter of the mini-slinger such that it approaches quite close to the angled groove in the block. The pics don't show just how close it really is. For those who wonder if the mini-slinger will be enough, remember that the 2-piece seal motors originally used a rope seal, which were little more than dirt wipers. The modern neoprene seals work quite well as long as they are properly installed (and the CDR valve isn't plugged). With it's close distance to the block and tapered edge I doubt much oil will migrate past it.
Here's what I did. First, I mounted the crank in the 3-jaw chuck and supported the snout end with a live center. Then an indicator was used to check runout on both ends, and adjustments were made until runout was less than .001". Then, I checked the runout of the center main journal to check for warpage. You can imagine my dismay when the indicator read .0045

. The spec is .0025 or less, and ideally you want less than .001". We had the ends indicated in to only a few tenths runout, so if the crank was straight it should have read less than .0025". After some rechecking and coming up with the same reading over and over, I figured the crank was junk. Then my friend had a realization. He relaxed pressure on the live center and we spun the crank again. The indicator read .0004"!!! Less than half a thou of runout

. The pressure of the live center flexed the crank that much. So, with the crank confirmed to be straight, I started hacking away.
The rough machining was done with a diamond-shaped carbide insert. Once I got down to the diameter of the mini-slinger, I switched to a .160" wide carbide grooving insert and snuck up to within .010" of the finished diameter, I also left steps in each corner for radii. The final cuts were made with another carbide insert which my friend ground into a .093" radius. I removed the steps and .008" of the remaining material, leaving me with .002 material and nice radii in the corners. Finally, I polished the seal surface in stages. I started with 80 grit cloth sanding tape, and then after I got it as smooth as possible (and .0005" smaller) I went to 400, then to 800, and finally for grins finished up with 1200 grit. The surface is mirror smooth, although it doesn't look like it in the pics since it is coated with oil and a few dust particles.
Here's some more pics of the crank in the block. BTW, the "bearings" are pieces of cardboard. I haven't got the actual bearings yet:
I also deburred and radiused bolt holes and the edges of the bulkheads. Basically, anyplace a stress riser could form:
The final bit of good news is that my machinist friend has also started CNCing my stud girdles Right now only one is partially roughed. The roughing end mill he was using was already in poor shape when he started, and it gasped its last after an hour of noisy cutting, so he decided to call it a day (that was Friday evening). He should be able to resume carving on them Monday afternoon, and hopefully they will be done by the end of the week. Then I can send the block off to the machine shop for boring and honing. I will also have the line bore rechecked and honed if it is needed.
Yup, piece by piece it is coming together
