I pulled the shaft this morning and swapped in a brand new Spicer non cross drilled u-joint. It was a definite improvement, but the vibration is still there and gets progressively worse. I let off at 90 this time, but it was getting pretty bad still.
I sent an e-mail to Gearstar, I measured play on the output yoke, .012" fully inserted and about .023" pulled out about 1.5" which is about where it sits at ride height. That seems a bit excessive to me, I thought the roller bearing output would be tighter than the bronze bushing, but apparently not.
I sent an e-mail to Gearstar, I measured play on the output yoke, .012" fully inserted and about .023" pulled out about 1.5" which is about where it sits at ride height. That seems a bit excessive to me, I thought the roller bearing output would be tighter than the bronze bushing, but apparently not.
... I'm hoping they get it fixed for me later today, but it may not be until tomorrow.