so lot has happened, here is the recap from the other forum.
Picked it up today!! The baattery had to be swapped over to my spare, the timing still aint right, and the oil needs to be changed. I had to pay $1000.00 more so the total out the door was 4k.
It has a bad flat spot, and need some serious tuning, but it does run great cruising down the road. I got some weird noise under a load, almost like the fan is hitting the shroud, but it's not that sounds like it coming from the back of the engine somewhere?? Oh well I will figure it out tomorrow and see waht id goin on. Wouldnt say I was happy yet, but glad it's back in my hands, will make a video and pics tomorrow.
well seems to have all the same issues as befor with a few new ones.
Vacum is low and erratic, and the small miss is still there can hear just barely. In addition there seems to ba huge vacum leak somewhere, the battery went bad, the odd noise coming from the tranny or converter or flexplate when you put it under a load. and it seems the trany lins got into the drive shaft and one is ready to break.
So I tried setting the timing but havent drove it yet due to the tranny line issue. I set it at 10 degrees, then backed the vacum advance down to 14 degrees and is seemed a little better in the driveway. I tried adjusting the carb to idle it down, and it wont drop below 1k rpm, the A/F mixture screwes dont seem to have any effect either, can turn them in all the way and it still runs, it should die if I do that. So yeah got a few problems to sort out now. I do still think the engine is good and can be awesome after i get through all the other issues.
To top it off it's colder than **** here so jut misrable to try and work on it. My main concern is the tranny noise?? Dont understand that one at all, it did not do that before so I am at a loss as to how he could have made this start??
Just pissed off now and frustrated, got to stop and chill for a day or two and start back on it easy like. Will start with the trans lines and go from there.
guess I better load some pics and stuff huh!
tranny lines all in the wrong place kinda hard to see but there is the smash
some video up next
well while waiting for that to load.............
I patched the line and it still did it a little but decided to go drive it, not much power at all! (scary) but it sorta got better, then came home and tried to make the noise again and it didnt? well it spun both back tires and left some little divits to sit in but no noise, so wanna drive it again, go to back up and cant pull out of the 1" deep holes??? what the F, got out checked the trany fluid again and yep right where it's supposed to be. I get back in and manage to get back up finally and drive off for a longer drive, it seems ok but still no real power at all. I went down the highway running bout 65 and it is smooth as silk, when I mash it it speeds up no loud knocking noise and feels purdy good.
I get turned around and stand on it, shift to second still pulling good (not evil good) but pulling, then hit third and never let off. I watch the speedo go past 85 and keep going, and switch to the tach and watch it climb to 5500 rpm before I let off, and it was still pulling the same!! Prolly around 120-130 mph! I ease back down and oil press is still 60, temp is 185, trans temp is 155. Still seems good but dang I am starting to think it may be trans related??
oh here is the knocking under load.
next video is of the cam rumble, and tried to make the noise as above and it dies on me then cant get it started again.
Also the miss seems to have disappared? didnt recheck the vacum again, and plan to put the new battery and fix the crappy wiring, if that solves the starter issues then good if not, got to try and shim the starter or just buy a new one that is smaller but high torque! Havent heard any pinging but need to get gas so gonna throw in the 104 octane booster to see what that does. Also gonna order the mechanical fuel pump to, but will wait to see if I need a starter too so can order it all at once.
So to sum up I am lost on what the noise is, and it seems to have gone somewhat? The plug wires seem good now, but the timing and carb are not adjusted right I am sure of it. Much as I hate to think about it I might take it to another shop that has a sunpro computer to hook up to it and run some diognostics. Might even have it adjusted by someone if I can figure it out. I still think it has a big vacume leak causing issues so need to track that down first I guess.
ok well here is the last video of the day

and I guess it has a posi by the looks of the divits!!
ok so cant find the battery cables I want to fix the starting issues. So I just ordered 20' of 2 AWG in red and 20' in black, a hammer crimper, 5 copper lugs of each of these terminal sizes, 1/4, 5/16,3/8, and 1/2. Now just gotta get these
5 bucks for a set at the local Big R hardware. Then still need to get a solenoid and relay, and switch to hook up the dual battery set up.
or I might get this
http://www.summitracing.com/parts/PRF-40102/[/URL] I think I can put the parts together for cheaper than that maybe. The main thing is I want to be able to flip the switch and apply full power of both batteries to the starter when it is hella cold and make it start easy. Guess I should get a better starter too, but that will come later, main thing I want for now is to get all my electrical mess sorted out once and for all. Then get to the rest.
Also got the new mechanical fuel pump on the way along with 25' of 3/8" stainless steel braided hose. Gonna replace all the tranny lines, cooler lines, filter lines and rubber fuel lines that I got running all around the place. I still need to sort out the new lines for the engine oil cooler too, but that is down the road a bit since I am not driving it anyway. I will start looking for any vacum leaks while I am cleaning up the wiring and painting the engine compartment. Just to much ugliness going on in there, that is prolly what it dont wanna run right, need to get all the half ass out and do it all correct!!
figured I better throw in the starting of the project. more to come tomorrow.
what a mess!!
totally half ass on the positive side!!
lots of clutter and just ugly!
first step done!