check the ignition switch, there was a recall on that switch, should have been done. Now the recall switch is 20 years old, and I never saw a big improvement over the old design.
the switch starts to separate then the shuttle misses contact with some or all of the circuits. At worse it shorts to ground and starts a fire.
Is on the column behind knee bolster. Time for under dash yoga stretches
I'm pretty certain it's fuel related, injectors not firing on crank... i ran the rig REAL low on oil.. was down about 4 qrts.. these motors are notorious for needing good oil and not stoopid low like that... i'm hoping now that i topped it off and have been running it some, it'll help clear any issue the hpop system was having.. gonna try to get it running again now, and let it idle in the driveway for an hr.. this weekend i'll check the level in the hpop ressy..
I'm actually thinking of getting an economical obd2 reader for the rig... not that it's throwing a CEL, but...
good job Rog!
and the last wasn't tough to break free... had to go to Ace... 