
Don’t put that sh*t on me Ricky Bobby! Nobody told you to drive down that dry wash in the dark!After lunch, got bearings and hubs lubed up and installed, locking cap on. Axles lock and unlock.
Found a piece of 3/4 .120 wall tube I can chop up to make the spacers for the 2nd cross member.
Set it down on body stands to check drag link angle. With raise steering arm and stock pitman arm it is almost level. I noticed it is bent to, I think that happened while I was out with Zoo. Steering wheel was straight going wheeling Zoo and not straight.
I have a new arm end, may plop down $$$ for ORD coupler.
edit: forgot picture, I was in pool while I posted above
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I was just messing with you. It’s all good. If you aren’t using it stuff can’t get tweaked. I was happy to see you out with it for sure. Plus the search and rescue mission in the dark was a bonus. If you didn’t have that million candle power spot light I don’t think we would have found you so quickly. Bill and I got a kick out of heading out in the dark looking for you.Not saying it was you, I am say I went wheeling with you, and bent my stuff, been that for a year, I noticed the wheel center change right away. At first I was worried frame was cracked, frame is good, so it has to be the bent end. I have a coupler and long end otw and got a short side on closeout from RA awhile back. Yeah I did drive down some rough trails in the dark trying to find you guys. That deep sandy ass wash was to soft to bend stuff.
Once again I shoulda bought light bars instead of winch. Now I have a real drive shaft, can't wait to test it, fingers crossed have enough clearance on that trans pan.
Is all good on my end Rob no blaming here
That’s gotta feel good. Other than the hot air haha.After charging the battery over night, burb cranked right over and lit off, but was running stupid rich, I fiddled with the choke and tapped lightly on the bowl while running but just wouldn't clean up and stalled. Well there was fuel coming out of the accelerator pump stem, off came the air horn, I didn't see any reason for the flooding. Float hadn't sunk, needle and seat looked clean. I went ahead and changed the float I had ordered a nitrophyl (alcohol resistant) float.
Set at 15/32nd. Change the primary metering jet rod spring to next strong. Think I have a lean condition at cruise, this might help lift the rods a little earlier under medium vacuum.
fire her up again choke works perfect, no soot out the tail pipe, idle is low when off the choke. Swap cars around get Honda on lift, and go to parts store in 77. Runs well no stumble at stops from low idle, charging volt is low at in gear idle, 2 a/c hi blowers, condenser fan, trans cooler fan, fuel pump, and center consul cooler all running. 14.3v main,13.8v aux, idle in park, no a/c. A/c works but not well, probably low again. It has been months, maybe a year, since I touched it. It did cool, After my lunch stop inside truck was 110, short drive to parts store, down to 90, 6ish mile home got to 80. 105 by my weather at at the time. Engine temp under mid point on gauge, trans temp 185ish, oil pressure 5/8th on gauge. All good, trans fill was tad low still need another quart.
Am chomping at the bit to get her out in the soft stuff and engage the front diff, with the driveshaft. hopefully in next couple days I will be able to get to it.
So any onions on how to break in new gears in a front part time axle ??? Same type heat cycles ?

So any onions on how to break in new gears in a front part time axle ??? Same type heat cycles ?
